主办:陕西省汽车工程学会
ISSN 1671-7988  CN 61-1394/TH
创刊:1976年

汽车实用技术 ›› 2022, Vol. 47 ›› Issue (18): 153-158.DOI: 10.16638/j.cnki.1671-7988.2022.018.031

• 工艺装备 • 上一篇    

啮合套渗碳淬火变形控制

丁福明,秦鹏涛,罗沭东   

  1. 陕西汉德车桥有限公司
  • 出版日期:2022-09-30 发布日期:2022-09-30
  • 通讯作者: 丁福明
  • 作者简介:丁福明(1979-),男,工程师,研究方向为热处理变形控制,E-mail:sqdfm79@sina.com。

Deformation Control of Carburizing and Quenching of Sliding Sleeve

DING Fuming, QIN Pengtao, LUO Shudong   

  1. Shannxi Hande Axle Company Limited
  • Online:2022-09-30 Published:2022-09-30
  • Contact: DING Fuming

摘要: 啮合套是汽车驱动桥轮间差速锁机构的重要零件,在使用过程中会受到相关件的冲击 载荷作用,所以在设计产品时会要求对啮合套采用渗碳淬火处理以提高其强度。生产过程中 发现,产品渗碳淬火处理过程会导致 50%的工件变形,花键跨棒距尺寸不合格,无法装配报 废处理。为了控制啮合套加工过程中的变形,通过加工过程跟踪和大量的实验数据分析,判 定造成工件变形、不合格的主要原因为装炉方式不合理。工件散装四周相互抵压,在完全奥 氏体化后工件强度降低,抵压导致工件产生变形;同时在淬火过程中工件受外力作用,导致 跨棒距收缩量不一致,椭圆和稍度超差。通过研究工件的装炉方式,增加隔层,消除工件之 间的相互抵压受力和改变摆放姿态,有效地控制了工件变形量,保证渗碳淬火后工件变形可 控,符合工艺要求,合格率达到了 100%。

关键词: 啮合套;渗碳淬火;变形控制;变形量;摆放姿态

Abstract: Sliding sleeve is an important part of the differential lock mechanism between the wheels of the automobile drive axle, which will be affected by the impact load of the relevant parts in the process of use, so it is required to adopt carburizing and quenching to improve the strength of the sliding sleeve in the product design. In the production process, it was found that the carburizing and quenching process of the product would lead to 50% of the workpiece deformation, and the size of spline span bar distance was not qualified, so it could not be assembled and scrapped. In order to control the deformation of sliding sleeve in the process of machining, the main reason for the deformation and disqualification of workpiece was determined by the process tracking and a large number of experimental data analysis. The workpiece in bulk was counterpressed around each other, and the strength of the workpiece was reduced after the complete austenitizing, and the counterpressure led to the deformation of the workpiece. At the same time, during the quenching process, the workpiece was subjected to external forces, resulting in inconsistent shrinkage of the span bar distance, and the ellipticity was out of tolerance. By studying the way of loading the workpiece, increasing the layer, eliminating the mutual resistance force between the workpiece and changing the placement posture, the deformation of the workpiece was effectively controlled, to ensure that the deformation of the workpiece after carburizing and quenching was controllable. In line with the process requirements, the qualified rate reached 100%.

Key words: Sliding sleeve; Carburizing and quenching; Deformation control; Deformation; Placement posture